SlideShare una empresa de Scribd logo
1 de 39
Descargar para leer sin conexión
Deepwater Horizon Investigation




                             Deepwater Horizon Accident Investigation   1
Investigation Context

   Terms of Reference


   Investigation Team


   Data and Analysis


   Investigation Limitations




                               Deepwater Horizon Accident Investigation   2
Eight Barriers Were Breached
                              Well integrity was not established or failed
            6             7     − Annulus cement barrier did not isolate hydrocarbons
                                1
                3     5
                                − Shoe track barriers did not isolate hydrocarbons
                                2


                              Hydrocarbons entered the well undetected and
        Riser
                  4             well control was lost
                                − Negative pressure test was accepted although well
                                3
              8
                                  integrity had not been established
            BOP
Sea Floor                       − Influx was not recognized until hydrocarbons were in
                                4
                                  riser
                                − Well control response actions failed to regain control of
                                5
       Casing
                                  well

                              Hydrocarbons ignited on the Deepwater Horizon
                                − Diversion to mud gas separator resulted in gas venting
                                6
                                  onto rig
                                − Fire and gas system did not prevent hydrocarbon
                                7
                                  ignition

                              Blowout preventer did not seal the well
                      1
     Reservoir                  − Blowout preventer (BOP) emergency mode did not
                                8
                                  seal well
                      2                                Deepwater Horizon Accident Investigation   3
Introduction
Technical Presentation




                    Deepwater Horizon Accident Investigation   4
Well Integrity Was Not Established
              or Failed




                        Deepwater Horizon Accident Investigation   5
Production Casing Installation
                                                                   After drilling to total depth, casing is run to
                                                                   bottom in preparation for the cement job. A
     Choke
                                                                   double valve float collar is used to prevent
                                                    Kill
     Boost                                                          backflow or ingress of fluids through the
                                                                    shoe track until the cement hardens and
                                                                           creates a permanent barrier.
             BOP
                                                                       April 18th 00:30 – April 19th 19:30
Sea Floor                                         17:30 – 19:30      Long string design robust, consistent with
                                                Circulated prior
       Cement      36”                           to cement job       similar wells in the area
       Mud                                                           9 attempts made to establish circulation
                    28”

       Spacer
                                                                     to convert float valves
                     22”

                                                                     Circulate ~6 times open hole volume,
                     18”

                                                                     limited circulation due to concerns over
                          16”
                                                                     creating losses and hole washout
                     13-5/8”

                                                                     No evidence that hydrocarbons entered
                         11-7/8”
                                                                     the wellbore prior to the cementing
                          9-7/8”
                                                                     operation
    14.17 ppg
     SOBM


                                           Primary reservoir
                                                 sands
                                               (12.6 ppg)

                                   Bottoms–up
                                   Marker
                                                                         Deepwater Horizon Accident Investigation    6
Cement Job
                                                                                             Cement is pumped down casing through
                                                                                              the float collar and up the annulus to
                                                                                               isolate the primary reservoir sands.
     Choke                                    Pull out of hole
                                                        Kill                                     April 19th 19:30 – April 20th 07:00
     Boost                                     with running
                                               tool and drill                                 Nitrogen cement slurry chosen
                                                    pipe
                                                                                                 – To achieve light weight slurry due to
             BOP                                  Set and test                                     limited pore pressure / fracture
                                                 casing hanger
                                                 seal assembly
                                                                                                   gradient window
Sea Floor
                                                           00:35 – 02:50
                                                                                              Possible risk
                         36”                    Drill-Quip seal assembly installed               – Stability of foam
     Base Oil                                         and successfully tested.
                                                            Centralizer
                                                 No lock down sleeve installed.                  – Relatively small volume
     Spacer               28”

                                                           02:50 – 07:00                         – Susceptible to contamination
     Cap
                                                   Pull out hole with drill pipe.
     Cement                 22”                                                               Mitigation of risk by
     Foamed                  18”
                                                                                                 – Thorough testing of slurry design
     Cement
                                            Bottoms–up
                                16”         Marker                                               – Precise placement
     Tail Cement
     Mud                    13-5/8”                                                           Centralization
                                                   Primary
     Nitrogen                  11-7/8”
                                                  Reservoir                                      – 6 inline centralizers spaced across
     Breakout                                       Sands                                          the reservoir sands
                         Shoe – 17,168’
                                                  (12.6 ppg)
                                                  Top of
                                9-7/8”       cement 17,260’                                      – Additional centralizers not run
                                                                                                   because incorrectly thought to be
                                                                                                   wrong type
                                                                         Primary reservoir
                   Float Collar – 18,115’   6 centralizers                     sands             – Risk of channeling above reservoir
                                                                             (12.6 ppg)
                                                                                                   sands known and accepted
                         Shoe – 18,304’
                                                                                                 Deepwater Horizon Accident Investigation   7
Key Finding #1
The annulus cement barrier did not isolate the reservoir hydrocarbons
                                                                                             Cement is pumped down the
                                   Cement Slurry Placement                                landing string and casing into the
                                                              Base Oil
                                                                   ppg
                                                              16.7ppg
                                                               6.7
                                                                                           annulus to isolate hydrocarbon
                                                                                                   bearing sands.
                                                               Spacer
                                                              14.3 ppg
Riser                                                         14.3 ppg
                                                                Cap
                     Cement                   Mud
                   Channeling                                 16.74 ppg
                                                                                                 Foam slurry recommended was a
                                           14.17 ppg             Cap
                                                               Cement
                                                                                                 complex design
                                                              16.74 ppg


BOP
                                                                                                 Risk of contamination using small
Sea Floor                                                      Foam                              volume of cement
                                                              Cement
                                                               Foam
                                                              14.5 ppg
                                                              Cement                             No fluid loss additives
                                                              14.5 ppg
                                                                                                 Incomplete pre-job cement lab
Casing                                                                    Centralizers
                                             Spacer                                              testing
                                            14.3 ppg
                                                                                                 Foam slurry was likely unstable
                    Float Collar
                                            Top Wiper Plug
                                          Top Wiper Plug                                         and resulted in nitrogen breakout
                                          Bottom Wiper Plug
                                         Bottom Wiper Plug       Shoe

                   Tail Cement                                   Track
                    16.74 ppg                                                12.6 ppg    Shoe
                                                                                         Track




Reservoir          Reamer Shoe                                             Tail Cement


                 Nitrogen Breakout
                                                                                             Deepwater Horizon Accident Investigation   8
Cement Slurry Design Issues


                                       An independent lab completed over 500
                                       tests on a representative cement slurry and
                                       reported the following:

                                         50% quality foam at surface conditions
Original Height
                                         was not stable
                                         18.5% quality foam (downhole quality)
                                         was not stable
                                         Yield point of the Halliburton slurry was
                                         too low for the foam cement (2 lb / 100 ft2
 Final Height                            yield point at 135 deg F)
                                         Fluid loss for the base slurry was
                                         excessive compared to industry
                                         recommendations (302 cc versus 50 cc
                                         per 30 min)
 Cement

                                       Note: QUALITY = Nitrogen Volume /
                                         (Nitrogen + Base Slurry Volume)




        Unstable Foam Sample
                                            Deepwater Horizon Accident Investigation   9
Flow Through Shoe Track - Supporting Evidence

                          Casing    Key Observations for Flow Seal
                           Shoe      Through Shoe vs. Seal Assembly
                          Failure          Assembly           Failure

                           Y        Mechanical Barrier
                                    Failure Mode Identified       Y
                           Y
                                    Realistic Net Pay
                                    Assumption                    N
                           Y
                                    1400 psi recorded on
                                    drill pipe during negative    N
                                    test at 18:30

                           Y
                                    Ability to flow from
                                    20:58                         N
                           Y
                                    Pressure Increase from
                                    21:08 to 21:14                N
 16ppg Spacer              Y
                                    Pressure Response from
                                    21:31 to 21:34                N
 14.17ppg SOBM (Mud)
 8.6ppg Seawater
 Influx
                           Y
                                    Timing for Gas Arrival to
                                    Surface                       N
                                                                                                   Seal
                                                                  N
                Casing              Static Kill
                 Shoe
                Failure
                           Y                                                                     Assembly
                                                                                                  Failure




                                                                 Deepwater Horizon Accident Investigation 10
Key Finding #2
The shoe track mechanical barriers did not isolate the hydrocarbons
                                                     Tail cement is displaced down the casing
                                                       into the shoe track. The tail cement is
                                                         designed to prevent flow from the
                                                     annulus into the casing. The float collar
                                                      valves, which provide a second barrier,
     Riser
                                                      must close and seal to prevent flow up
                         Hydrocarbon Flow                            the casing.
                               Path
                                                       Shoe track had two types of mechanical
     BOP                 Float Collar
                                                       barriers: cement in the shoe track and the
    Sea Floor
                                                       double check valves in the float collar
                                                       Shoe track cement failed to act as a
                 Check Valves
     Casing                                            barrier due to contamination of the base
                                                       slurry by break out of nitrogen from the
                                                       foam slurry

                 Shoe track cement
                                                       Hydrocarbon influx was able to bypass
                                                       the float collar check valves due to either:
                                                             Valves failed to convert or
                                                             Valves failed to seal
                      Centralizers
                                                       Flow through shoe confirmed by fluid
                                                       modeling and Macondo static kill data

     Reservoir



                                        Flow Ports
                                                          Deepwater Horizon Accident Investigation 11
Hydrocarbons Entered the Well
Undetected and Well Control Was Lost




                        Deepwater Horizon Accident Investigation 12
Casing (Positive) Pressure Test
                 2700
                  psi




                        Kill
                                                 A positive pressure test verifies the
                                                   integrity of the casing and seal
                                                              assembly.

                                                      April 20th 07:00 – 12:00
 Sea Floor
                                                 Casing was pressure tested to:

        Cement
                                                      250 psi (low)
        Mud                                           2700 psi (high)
        Spacer                                   Test successful
                                                 Proved integrity of blind shear rams, seal
                                                 assembly, casing and wiper plug
                                                 Test does not test the shoe track due to
                                                 presence of wiper plug




                                   Primary
                               reservoir sands


                                                    Deepwater Horizon Accident Investigation 13
Negative Pressure Test
                                                                  The negative-pressure test checks the
                                                                  integrity of the shoe track, casing and
                                                                 wellhead seal assembly. This simulates
     Choke
     Boost
                          Kill
                              15:04 – 15:56                            conditions during temporary
                         Seawater pumped into                    abandonment when a portion of the well
                       Boost, Choke, and Kill lines
                                                                         is displaced to seawater.
             BOP
                                                                        April 20th 15:04 – 19:55
                     16:54 - Close Annular

Sea Floor
                                                                   Negative test simulates underbalanced
                             15:56 – 16:53
                          424 bbls of 16 ppg
                                                                   condition
                     spacer followed by 30 bbls
       Cement        of freshwater and 352 bbls
                                                                   Spacer used between mud and seawater
                   of seawater pumped into well
       Mud                                                         Leaking annular at start of test moved
       Spacer         16:54 – 16:59                                spacer across kill line inlet
                    50 bbls bled off
       Seawater     drill pipe due to                              Negative test started on drill pipe but
       Influx       leaking annular                                changed to kill line
                                                                   Bleed volumes higher than calculated
                                                                   Drill pipe built pressure to 1400 psi with
                                                                   no flow on the kill line




                                             Primary reservoir
                                                   sands
                                                 (12.6 ppg)



                                                                      Deepwater Horizon Accident Investigation 14
Negative Pressure Test
                                                                                 The negative-pressure test checks the
  17:52 – 18:00                                                                  integrity of the shoe track, casing and
    Open kill
line to conduct                                                                 wellhead seal assembly. This simulates
       Choke
  negative test                         Kill                                          conditions during temporary
      Boost

                                             16:59 – 17:08                      abandonment when a portion of the well
Bled 3 - 15 bbls
  into kill line
                                          Annular seals with                            is displaced to seawater.
                                         increased hydraulic
              BOP
                                           closing pressure
 Flow did not                                                                          April 20th 15:04 – 19:55
   stop and
                                    Fill riser with 50 bbls of mud
  “spurted”                                                                       Negative test simulates underbalanced
 Sea Floor

Kill line closed
                                           17:08 – 17:27                          condition
                                         Monitored that the
        Cement
                                          annular sealed                          Spacer used between mud and seawater
        Mud                              17:27                                    Leaking annular at start of test moved
                                    Bled 15 bbls of                               spacer across kill line inlet
        Spacer
                                seawater from drill pipe
        Seawater                                                                  Negative test started on drill pipe but
                                  Decision made to
        Influx                  change test to kill line                          changed to kill line
                                                                                  Bleed volumes higher than calculated
             Cement
              Tank     Total
                                                                                  Drill pipe built pressure to 1400 psi with
                      Volume
                                                                                  no flow on the kill line

                      15 bbls




                                                            Primary reservoir
                                                                  sands
                                                                (12.6 ppg)



                                                                                     Deepwater Horizon Accident Investigation 15
Negative Pressure Test
                                                                                              The negative-pressure test checks the
                               1400       0                                                   integrity of the shoe track, casing and
                                psi      psi
                                                        18:00 – 18:35                        wellhead seal assembly. This simulates
     Choke                                     Drill pipe pressure gradually
     Boost                                         increased to 1400 psi
                                                                                                   conditions during temporary
                                                                                             abandonment when a portion of the well
                                                          18:42
                                                                                                     is displaced to seawater.
             BOP                                    Pumped into kill
                                                  line to confirm full                              April 20th 15:04 – 19:55
                                                 Kill line opened for
Sea Floor                                      monitoring negative test                        Negative test simulates underbalanced
                                                                                               condition

       Cement                                       18:42 – 19:55                              Spacer used between mud and seawater
                                            Monitored kill line for 30 min
       Mud                                 1400 psi on drill pipe described                    Leaking annular at start of test moved
                                               as a “bladder effect”                           spacer across kill line inlet
       Spacer
       Seawater                                         19:55
                                                Negative pressure test
                                                                                               Negative test started on drill pipe but
       Influx                                     was concluded and                            changed to kill line
                                                considered a good test
                                                                                               Bleed volumes higher than calculated
            Cement
             Tank     Total
                                                                                               Drill pipe built pressure to 1400 psi with
                     Volume
                                                                                               no flow on the kill line
                     18 bbls          Additional
                     15 bbls          3 bbl influx



                                                                         Primary reservoir
                                                                               sands
                                                                             (12.6 ppg)



                                                                                                  Deepwater Horizon Accident Investigation 16
Key Finding #3
The negative pressure test was accepted although well integrity had
not been established


                                                     1400    0
                                                      PSI   PSI
     Riser



                      Choke                                        Kill    Bleed volumes not recognized as a
                      Boost

                                                                           problem
     BOP
    Sea Floor

                              BOP
                                                                           Anomalous pressure on drill pipe with no
                 Sea Floor
                                                                           flow from kill line
                                                                  Spacer
     Casing         SOBM                                                   Test incorrectly accepted as successful
                    Spacer
                    Seawater                                               Negative testing not standardized
                    Influx




                                    Shoe – 17,168’


                                    TOC – 17,260’



                                      FC – 18,115’

     Reservoir

                                    Shoe – 18,304’

                                                                                Deepwater Horizon Accident Investigation 17
Well Monitoring – Driller’s Console and Mudlogging unit


                                  Well monitoring is performed to understand if
                                  the well has losses or gains

                                  Driller is responsible for monitoring and
                                  shutting in the well

                                  The mudlogger provides monitoring support to
                                  the driller

                                  Displays and trending capability available in
                                  both Driller’s and Mudlogger’s cabins

                                  Flow, pressure and pit sensors can indicate
                                  flow

                                  Simultaneous activities were taking place on
                                  April 20th to prepare for rig move

                                  Standards for monitoring do not specifically
                                  address end-of-well activities




                                           Deepwater Horizon Accident Investigation 18
Undetected Flowing Conditions
                                                                   Mud in the riser is displaced with
                                                                 seawater in preparation for temporary
                                                                            abandonment.
     Choke                 Kill

     Boost                         21:08
                         Spacer arrived at surface                        April 20th 19:55 – 21:14
                           Shut pumps down
                              for sheen test
             BOP                                                 20:02 Resume displacement of mud with
                                 20:02                           seawater
Sea Floor
                           Annular opened
                            after negative
                                  test
                                                                 20:52 Well becomes underbalanced and
                                                                 starts to flow
     Cement                     20:00 – 21:08
                           Resumed pumping
     Mud              Displaced riser with seawater              After 20:58 gain being taken and pressure
     Spacer              until spacer is at surface
                                                                 begins increasing
     Seawater
                                20:52                               – Flow from well masked by emptying
     Mud + Seawater   Well becomes underbalanced
                                                                      of trip tank
     Mix
     Influx                                                      21:08 Pumping stops for sheen test
                                                                    – Pressure increases with pump off
                         20:58 - 21:08
                          39 bbl gain                            21:14 Sheen test complete, displacement
                                                                 resumes

                                             Primary reservoir
                                                   sands
                                                 (12.6 ppg)



                                                                      Deepwater Horizon Accident Investigation 19
Key Finding #4
The influx was not recognized until hydrocarbons were in the riser
                  2000                                                                                                                              3000
                                                                                   Flow Indications
                                                                                   Based on Real-time Data                                                                       Flow indications:
                                                    Flow Out (calibrated)
                  1800
                                                    Flow In (rig pumps)
                                                    DP Press (rig pumps)
                                                                                                                                                    2500                               #1: Drill pipe pressure
                  1600
                                                                                                                                                                                       increased by 100 psi,
                                                          Decreasing trend should
                  1400                                                                                                                                                                 (expected decreased);




                                                                                                                                                           Pump Pressure (psi)
                                                              have continued                                                                        2000
                                                                                                                                                                                       ~39 bbl gain from 20:58
Flow Rate (gpm)




                  1200
                                                                       Indication #1                                                                                                   to 21:08
                  1000                                                                                                                              1500

                   800
                                                                                                                                                    1000
                   600

                   400
                                    20:52-Flow starts                                                                                               500
                   200

                  Cumulative Gain
                     0
                                                     0                                  39                                            300           0
                                                    bbl                                 bbl                                           bbl
                         20:45



                                            20:50



                                                            20:55



                                                                       21:00



                                                                                21:05



                                                                                              21:10



                                                                                                      21:15



                                                                                                              21:20



                                                                                                                      21:25



                                                                                                                              21:30



                                                                                                                                            21:35
                                                                    1,017 psi




                                 SOBM (mud)
                                 Seawater
                                 Influx
                                 SOBM + seawater mix



                                                          21:08



                                                                                                                                               Deepwater Horizon Accident Investigation 20
Key Finding #4
The influx was not recognized until hydrocarbons were in the riser
                  2000                                                                                                                                                                3000
                                                                                   Flow Indications
                                                                                   Based on Real-time Data                                                                                                         Flow indications:
                                                    Flow Out (calibrated)
                  1800
                                                    Flow In (rig pumps)
                                                    DP Press (rig pumps)
                                                                                                                                                                                      2500                               #1: Drill pipe pressure
                  1600
                                                                                                                                                                                                                         increased by 100 psi,
                                                          Decreasing trend should
                  1400                                                                                                                                                                                                   (expected decreased);




                                                                                                                                                                                             Pump Pressure (psi)
                                                              have continued                                                                                                          2000
                                                                                                                                                                                                                         ~39 bbl gain from 20:58
Flow Rate (gpm)




                  1200
                                                                    Indication #1                                                                                                                                        to 21:08
                  1000                                                                                                                                                                1500

                   800                                                                                                                                                                                                   #2: Drill pipe pressure
                                                                                                                              Indication #2                                                                              increased by 246 psi with
                                                                                                                                                                                      1000
                   600
                                                                                                                       Overboard line opened                                                                             pumps off
                   400
                                    20:52-Flow starts                                                                  Flow out available only
                                                                                                                                                                                      500
                                                                                                                         to driller after 21:10                                                                            – Flow out does not
                   200
                                                                                                                                                                                                                             immediately drop
                  Cumulative Gain                    0                                  39                                                                              300
                     0
                                                    bbl                                 bbl                                                                             bbl
                                                                                                                                                                                      0                                      after shutting down
                         20:45



                                            20:50



                                                            20:55



                                                                       21:00



                                                                                21:05



                                                                                              21:10



                                                                                                                          21:15



                                                                                                                                      21:20



                                                                                                                                                    21:25



                                                                                                                                                                21:30



                                                                                                                                                                              21:35
                                                                                                                                                                                                                             pump
                                                                    1,017 psi
                                                                                                   1200                       Normal Flow Back
                                                                                                   1000                                       Flow Out
                                                                                              Flow Rate (gpm)




                                                                                                                                              Flow In
                                                                                                                800
                                 SOBM (mud)
                                 Seawater
                                                                                                                600
                                 Influx
                                 SOBM + seawater mix
                                                                                                                400

                                                                                                                200
                                                          21:08
                                                                                                                  0
                                                                                                                      16:50


                                                                                                                                  16:55


                                                                                                                                                17:00


                                                                                                                                                            17:05




                                                                                                                                                                                 Deepwater Horizon Accident Investigation 21
Key Finding #4
The influx was not recognized until hydrocarbons were in the riser
                  2000                                                                                                                                                      3000
                                                                                   Flow Indications
                                                                                   Based on Real-time Data                                                                                               Flow indications:
                                                    Flow Out (calibrated)
                  1800
                                                    Flow In (rig pumps)
                                                    DP Press (rig pumps)
                                                                                                                                                                            2500                               #1: Drill pipe pressure
                  1600
                                                                                                                                                                                                               increased by 100 psi,
                  1400
                                                                                                                                                  Indication #3                                                (expected decreased);




                                                                                                                                                                                   Pump Pressure (psi)
                                                                                                                                                                            2000
                                                                                                                                                                                                               ~39 bbl gain from 20:58
Flow Rate (gpm)




                  1200
                                                                    Indication #1                                                                                                                              to 21:08
                  1000                                                                                                                                                      1500

                   800                                                                                                                                                                                         #2: Drill pipe pressure
                                                                                                               Indication #2                                                                                   increased by 246 psi with
                                                                                                                                                                            1000
                   600
                                                                                                                                                                                                               pumps off
                   400
                                    20:52-Flow starts                                                                                                                       500
                                                                                                                                                                                                                 – Flow out does not
                   200
                                                                                                                                                                                                                   immediately drop
                  Cumulative Gain                    0                                  39                                                                    300
                     0
                                                    bbl                                 bbl                                                                   bbl
                                                                                                                                                                            0                                      after shutting down
                         20:45



                                            20:50



                                                            20:55



                                                                       21:00



                                                                                21:05



                                                                                              21:10



                                                                                                              21:15



                                                                                                                                  21:20



                                                                                                                                          21:25



                                                                                                                                                      21:30



                                                                                                                                                                    21:35
                                                                                                                                                                                                                   pump
                                                                    1,017 psi                                         1,200 psi
                                                                                                                                                                                                               #3: Drill pipe pressure
                                                                                                                                                                                                               increased by 556 psi with
                                                                                                                                                                                                               pumps off; ~300 bbl gain

                                 SOBM (mud)
                                 Seawater
                                                                                                                                                                                                          No well control actions taken
                                 Influx
                                 SOBM + seawater mix



                                                          21:08                                       21:31



                                                                                                                                                                       Deepwater Horizon Accident Investigation 22
Key Finding #5
Well control response actions failed to regain control of the well

                                                                                                                                         Influx enters riser
 3000           Based on Real-time Data                                                         First indication of well control response:
                                                                                               49 minutes and 1000 bbls after initial influx
                   Drill Pipe Presssure (psi)
 2500                                                                                                                                              BOP
                                                                 Mud shoots up derrick
                          Attempt to bleed                         -Diverter closed
                              pressure                              -BOP activated
 2000




                                                                                                            Explosion at 21:49
                                                  Close Drill Pipe
                                                                                 BOP Sealing
 1500

                                                                             Annular
                  Discussion about                                           leaking
 1000           “Differential Pressure”
                                                                                          - Mud and water raining onto deck
                                 Mud overflowing
                                  onto rig floor                                         - TP calls WSL, getting mud back,
  500                                                                                      diverted to MGS, closed or was
                  Pumps shut down                                                          closing annular

                                              Pressure increase due                      - AD calls Senior TP, Well blowing
    0                                         to annular activation                        out, TP is shutting it in now
        21:30

                  21:32

                             21:34

                                      21:36

                                                21:38

                                                         21:40

                                                                     21:42

                                                                               21:44

                                                                                       21:46

                                                                                                    21:48

                                                                                                                                 21:50
                                                                                                                            Deepwater Horizon Accident Investigation 23
Hydrocarbons Ignited on the
    Deepwater Horizon




                    Deepwater Horizon Accident Investigation 24
Diverting to the Mud Gas Separator at about 21:42
                                                                   12” Vent                    When responding to a well control event
                                                                                                the riser diverter is closed and fluids
                          6” Vacuum
                             Breaker                                                           sent to either the mud gas separator or
                                                            Bursting Disk                          to the overboard diverter lines.


                                                                                               Diversion to the MGS
                                                          MGS             Rated to 60 psi
                                                                          working pressure      Rig crew has the option to divert flow to
                                      Rotary
                                      Hose
     Mud                                                                                        port/starboard overboard lines or the
    System                             IBOP
                                                                                                MGS
                                                                                   Starboard
                                  Diverter                                         Overboard    Diverting to port or starboard will result in
                                                                                   Starboard
                                                                                                fluids venting overboard
     Port
Overboard          14” Diverter Line                        14” Diverter Line      Overboard

                                             Slip Joint         Rated to 100 or 500 psi         Liquid outlet from MGS goes to the Mud
              Overboard
               Caisson    Boost                             Kill
                                                                                                System under the main deck
                          Choke

                           BOP




     Seawater
     Seawater/Mud Mix
     Influx




                                                                                                    Deepwater Horizon Accident Investigation 25
Gas flow to Surface at high rate: 21:46 to 22:00
                                                                   12” Vent                 When responding to a well control event
                                                                                             the riser diverter is closed and fluids
                          6” Vacuum
                             Breaker                                                        sent to either the mud gas separator or
                                                            Bursting Disk                       to the overboard diverter lines.


                                                                                            Hydrocarbon flow from surface
                                                          MGS
                                                                                             equipment
                                      Rotary
                                      Hose
     Mud
                                                                                             Instantaneous gas rates reached
    System                             IBOP
                                                                                             165 mmscfd
                                                                                Starboard
                                  Diverter
                                                                                Overboard    Pressures exceeded operating ratings
                                                                                             (above 100 psi)
     Port                                                                       Starboard
Overboard          14” Diverter Line                        14” Diverter Line   Overboard
                                                                                             Gas would probably have vented from:
                                             Slip Joint
              Overboard
               Caisson    Boost                             Kill                                  Slip joint packer into the moon pool
                          Choke                                                                   12” MGS “gooseneck” vent
                           BOP
                                                                                                  6” MGS vacuum breaker vent
                                                                                                  6” overboard line through burst disk
     Seawater
                                                                                                  10” mud line under the main deck
     Seawater/Mud Mix
     Influx




                                                                                                 Deepwater Horizon Accident Investigation 26
Gas Dispersion across the Deepwater Horizon 21:46 to 21:50 hrs


                        Animation of Gas Dispersion



                         Upper Explosive Limit




                         Lower Explosive Limit

              3D View                            Cut Section Through Derrick Towards Aft




                                                           Deepwater Horizon Accident Investigation 27
Secondary protective systems did not prevent ignition
                                              Secondary protective systems are
                                               designed to reduce the potential
                                              consequence of an event once the
 3D view                                   primary protective systems have failed.

                           Fwd




Aft

Secondary Protective Systems
 Gas cloud reached the supply air
 intakes for engine rooms 3, 4, 5 & 6
 The Fire and Gas system did not
 automatically trigger a shutdown of the
 HVAC system for the engine rooms
 Limited areas of the rig are designated
 as electrically classified zones


                                               Deepwater Horizon Accident Investigation 28
Key Finding #6
Diversion to the mud gas separator resulted in gas venting onto the
                                                                  12” Vent
rig
                            6” Vacuum
                               Breaker                                                     When responding to a well control event
                                                          Bursting Disk                    the riser diverter is closed and fluids are
                                                                                            sent to either the mud gas separator or
                                                                                                to the overboard diverter lines.
                                                         MGS

                                     Rotary
                                     Hose                                                   Hydrocarbons were routed to the mud gas
       Mud
      System                          IBOP                                                  separator instead of diverting overboard
                                                                               Starboard    Resulted in rapid gas dispersion across
                                 Diverter                                      Overboard
                                                                                            the rig through the MGS vents and mud
                                                                                            system
       Port                                                                    Starboard
  Overboard          14” Diverter Line                     14” Diverter Line   Overboard

                                            Slip Joint
                Overboard
                 Caisson     Boost                         Kill


                            Choke

                             BOP

                                                                     BOP
                                                                   Sealed at
       Seawater                                                     21:47
       Seawater/Mud Mix
       Influx




                                                                                                Deepwater Horizon Accident Investigation 29
Key Finding #7
The fire and gas system did not prevent hydrocarbon ignition
 Gas Dispersion at 4 minutes
                                                Secondary protective systems are
                                                 designed to reduce the potential
       (Upper Explosive Limit)                  consequence of an event once the
                                                 primary protective systems have
                                          Aft                 failed.
                                                Gas dispersion beyond electrically
                                                classified areas
        Section through derrick
      3D view                                   Gas ingress into engine rooms via main
        (Lower Explosive Limit)
                                        Fwd
                                                deck air intakes

                                                The on-line engines were one potential
                                                source of ignition



                                  Fwd
   3D view
        Aft


    Aft

                                                    Deepwater Horizon Accident Investigation 30
Emergency Well Control System
    Did Not Seal the Well




                     Deepwater Horizon Accident Investigation 31
Blowout Preventer (BOP)
 BOP Control Panel


                                                         Surface HPU &
                                                         Accumulators              Flex Joint                              LMRP
                                                                               Upper Annular


                                                                                Lower Annular
                                                                            Stripping Element
                                     Mux Cable
                                     Hydraulic Conduit
                                                               LMRP
                                                            Accumulators

                                                                            Blind Shear Ram
                      Blue             Yellow
                     Control           Control
                                                                           Casing Shear Ram
                      Pod               Pod                                     (Non Sealing)
                                                                                  Upper VBR

                                                            Lower Stack          Middle VBR
                                                            Accumulators    Lower (Test) VBR
                                                                                                                           BOP
                                                                                                                           Stack
  Emergency Methods of BOP Operation Available on DW Horizon                         Wellhead Connector

         Manual                Automatic         ROV Intervention
                                                                                                     Wellhead
                                                   HOT Stab
         EDS
                                 AMF                  AMF                                  Sea Bed
     HP BSR Close
                                                   Auto-shear
                                                                                       Deepwater Horizon Accident Investigation 32
BOP Response (Before the Explosions)
                                                                BOP is designed to seal the wellbore and
                                                   20th
                                               April             shear casing or drill pipe if necessary.
                                         21:38 – Hydrocarbons
                                             enter the riser
                                                                April 20th
                                                                  21:41 annular BOP closed but appears
                                             Activation of
   Upper Annular
                                          Lower Annular BOP       not to have sealed the annulus

    Lower Annular
                                                                  21:47 a VBR likely closed and sealed the
Stripping Element
                                                                  annulus




 Blind Shear Ram

Casing Shear Ram                           Activation of VBR
     (Non Sealing)

       Upper VBR


      Middle VBR

Lower (Test) VBR




                Wellhead Connector




                              Wellhead



               Sea Bed                                                   Deepwater Horizon Accident Investigation 33
BOP Response (Impact of Explosions)
                                                               MUX cables provide electronic
                                                            communication and electrical power to
                                                                  the BOP control pods.

                                                           April 20th
                                                             Damage to MUX cables and hydraulic line
    Upper Annular

                                                                – Opening of annular BOP
     Lower Annular
                                          Annular BOP
 Stripping Element                       gradually opens
                                                             Rig drifted off location
                                                                – Upward movement of the drill pipe in
                                                                  the BOP
 Blind Shear Ram

Casing Shear Ram
     (Non Sealing)

       Upper VBR


      Middle VBR

 Lower (Test) VBR




                Wellhead Connector




                              Wellhead



               Sea Bed                                                  Deepwater Horizon Accident Investigation 34
BOP Response (After the Explosions)
                                                            There are several emergency methods of
                                                              activating the BSR to seal the well.

                                                            April 20th
                                                              EDS attempts failed to activate BSR
    Upper Annular
                                                              AMF sequence likely failed to activate BSR

     Lower Annular
                                                            April 21st – 22nd
 Stripping Element

                                         BSR activated by     ROV hot stab attempts to close BOP were
                                           Auto-shear
                                                              ineffective
                                                              ROV simulated AMF function likely failed to
 Blind Shear Ram                                              activate BSR
Casing Shear Ram
     (Non Sealing)                                            ROV activated auto-shear appears to have
       Upper VBR
                                                              activated but did not seal the well
      Middle VBR
                                                            April 25th – May 5th
 Lower (Test) VBR
                                                              Further ROV attempts using seabed
                                                              deployed accumulators were unsuccessful
                Wellhead Connector




                              Wellhead



               Sea Bed                                               Deepwater Horizon Accident Investigation 35
Key Finding #8
The BOP emergency mode did not seal the well
Explosions & Fire:                                                   The AMF provides an automatic
Loss of communication                                               means of closing the BSR without
Loss of electrical power                                                   crew intervention.
Loss of hydraulics

                                                                    EDS function was inoperable due to
                                        Damaged Hydraulic Conduit
                                                                    damage to MUX cables

                                      Damaged MUX Cable             AMF could not activate the BSR due to
                                                                    defects in both control pods

                                                                    Auto-shear appears to have activated
                     Blue             Yellow                        the BSR but did not seal the well
                    Control           Control
                     Pod               Pod
                                                                    Potential weaknesses found in the
                                                                    BOP testing regime and maintenance
                                                                    management systems


  Emergency Methods of BOP Operation Available on DW Horizon

        Manual                Automatic         ROV Intervention

                                                  HOT Stab
        EDS
                                AMF                  AMF
    HP BSR Close
                                                  Auto-shear
                                                                        Deepwater Horizon Accident Investigation 36
Summary of Findings and
  Recommendations




                Deepwater Horizon Accident Investigation 37
Recommendations
 25 Recommendations Specific to the 8 Key Findings


 BP Drilling Operating Practice and Management Systems
        Engineering Technical Practices and Procedures
        Further Enhance Deepwater Capability and Proficiency
        Strengthen Rig Audit Action Closeout and Verification
        Introduce Integrity Performance Management for Drilling and Wells Activities


 Contractor and Service Provider Oversight and Assurance
        Cementing Services
        Drilling Contractor Well Control Practices and Proficiency
        Oversight of Rig Safety Critical Equipment
        BOP Configuration and Capability
        BOP Minimum Criteria for Testing, Maintenance, System Modifications and Performance
        Reliability


 BP has accepted all the recommendations and is reviewing how best to implement across its
 world wide operations


                                                                     Deepwater Horizon Accident Investigation 38
Summary of Key Findings
                                 Well integrity was not established or failed
            6             7        − Annulus cement barrier did not isolate hydrocarbons
                                   1
                3     5
                                   − Shoe track barriers did not isolate hydrocarbons
                                   2


                                 Hydrocarbons entered the well undetected and
        Riser
                  4                well control was lost
                                   − Negative pressure test was accepted although well
                                   3
              8
                                     integrity had not been established
            BOP
Sea Floor                          − Influx was not recognized until hydrocarbons were in
                                   4
                                     riser
                                   − Well control response actions failed to regain control of
                                   5
       Casing
                                     well

                                 Hydrocarbons ignited on the Deepwater Horizon
                                   − Diversion to mud gas separator resulted in gas venting
                                   6
                                     onto rig
                                   − Fire and gas system did not prevent hydrocarbon
                                   7
                                     ignition

                                 Blowout preventer did not seal the well
                      1
     Reservoir                     − Blowout preventer (BOP) emergency modes did not
                                   8
                                     seal well
                      2                                   Deepwater Horizon Accident Investigation 39

Más contenido relacionado

La actualidad más candente

BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill
BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill
BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill Dhanish Ahsen
 
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...Mohanned Mahjoup
 
British petroleum & gulf oil spill of 2010
British petroleum & gulf oil spill of 2010British petroleum & gulf oil spill of 2010
British petroleum & gulf oil spill of 2010Aditi Podder
 
Deepwater Horizon Oil Spill Overview Presentation
Deepwater Horizon Oil Spill Overview PresentationDeepwater Horizon Oil Spill Overview Presentation
Deepwater Horizon Oil Spill Overview PresentationRichard Allaway
 
Well Completion Design.pdf
Well Completion Design.pdfWell Completion Design.pdf
Well Completion Design.pdfmmody4
 
Deepwater Horizon Oil Spill
Deepwater Horizon Oil SpillDeepwater Horizon Oil Spill
Deepwater Horizon Oil Spilltifftai
 
Well Control and Well Monitoring Systems
Well Control and Well Monitoring SystemsWell Control and Well Monitoring Systems
Well Control and Well Monitoring SystemsAFATous
 
Advanced blowout and well control robert d. grace
Advanced blowout and well control   robert d. graceAdvanced blowout and well control   robert d. grace
Advanced blowout and well control robert d. graceThần Chết Nụ Hôn
 
Completion equipment packer part #1
Completion equipment packer part #1Completion equipment packer part #1
Completion equipment packer part #1Elsayed Amer
 
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert Kampes
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert KampesAPSG35_Wellbores_and_Vertical_Reference_Levels - Bert Kampes
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert KampesBert Kampes
 
Petroleum Production Engineering - Perforation
Petroleum Production Engineering - PerforationPetroleum Production Engineering - Perforation
Petroleum Production Engineering - PerforationJames Craig
 
perforated joint, flow coupling and blast joint
perforated joint, flow coupling and blast jointperforated joint, flow coupling and blast joint
perforated joint, flow coupling and blast jointElsayed Amer
 
Liner hanger design and operations
Liner hanger design and operationsLiner hanger design and operations
Liner hanger design and operationsAbdulkadir Tekin
 

La actualidad más candente (20)

BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill
BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill
BP-Deepwater horizon-Macondo-Gulf Of Mexico Oil Spill
 
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...
UntitledExcessive Water Production Diagnostic and Control - Case Study Jake O...
 
Intelligent well completions
Intelligent well completionsIntelligent well completions
Intelligent well completions
 
British petroleum & gulf oil spill of 2010
British petroleum & gulf oil spill of 2010British petroleum & gulf oil spill of 2010
British petroleum & gulf oil spill of 2010
 
Deepwater Horizon Oil Spill Overview Presentation
Deepwater Horizon Oil Spill Overview PresentationDeepwater Horizon Oil Spill Overview Presentation
Deepwater Horizon Oil Spill Overview Presentation
 
Cementing
CementingCementing
Cementing
 
Well Completion Design.pdf
Well Completion Design.pdfWell Completion Design.pdf
Well Completion Design.pdf
 
Deepwater Horizon Oil Spill
Deepwater Horizon Oil SpillDeepwater Horizon Oil Spill
Deepwater Horizon Oil Spill
 
Well Control and Well Monitoring Systems
Well Control and Well Monitoring SystemsWell Control and Well Monitoring Systems
Well Control and Well Monitoring Systems
 
Wellheads and Flow Lines.pdf
Wellheads and Flow Lines.pdfWellheads and Flow Lines.pdf
Wellheads and Flow Lines.pdf
 
Sand control
Sand controlSand control
Sand control
 
Well intervention
Well interventionWell intervention
Well intervention
 
Advanced blowout and well control robert d. grace
Advanced blowout and well control   robert d. graceAdvanced blowout and well control   robert d. grace
Advanced blowout and well control robert d. grace
 
Bp oil spill
Bp oil spillBp oil spill
Bp oil spill
 
Completion equipment packer part #1
Completion equipment packer part #1Completion equipment packer part #1
Completion equipment packer part #1
 
blow out preventer system
blow out preventer systemblow out preventer system
blow out preventer system
 
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert Kampes
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert KampesAPSG35_Wellbores_and_Vertical_Reference_Levels - Bert Kampes
APSG35_Wellbores_and_Vertical_Reference_Levels - Bert Kampes
 
Petroleum Production Engineering - Perforation
Petroleum Production Engineering - PerforationPetroleum Production Engineering - Perforation
Petroleum Production Engineering - Perforation
 
perforated joint, flow coupling and blast joint
perforated joint, flow coupling and blast jointperforated joint, flow coupling and blast joint
perforated joint, flow coupling and blast joint
 
Liner hanger design and operations
Liner hanger design and operationsLiner hanger design and operations
Liner hanger design and operations
 

Destacado

Deep Water Horizon Accident Investigation Lessons Learned
Deep Water Horizon Accident Investigation Lessons LearnedDeep Water Horizon Accident Investigation Lessons Learned
Deep Water Horizon Accident Investigation Lessons LearnedSystems Engineering- DOE SPRPMO
 
Deepwater Horizon Oil Spill
Deepwater Horizon Oil SpillDeepwater Horizon Oil Spill
Deepwater Horizon Oil SpillJessica Goodman
 
BP's Deepwater Oil Spill Case Study Analysis - Business Ethics
BP's Deepwater Oil Spill Case Study Analysis - Business EthicsBP's Deepwater Oil Spill Case Study Analysis - Business Ethics
BP's Deepwater Oil Spill Case Study Analysis - Business EthicsÔn Thi
 
Deepwater Horizon Oil Spill: A Study of Behavioural Decision Making
Deepwater Horizon Oil Spill: A Study of Behavioural Decision MakingDeepwater Horizon Oil Spill: A Study of Behavioural Decision Making
Deepwater Horizon Oil Spill: A Study of Behavioural Decision MakingJerome Dauvergne
 
Operational Discipline - Deepwater Horizon Case Study
Operational Discipline - Deepwater Horizon Case StudyOperational Discipline - Deepwater Horizon Case Study
Operational Discipline - Deepwater Horizon Case StudyWilson Perumal and Company
 
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...Brad Keithley
 
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBA
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBABP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBA
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBAJonah Guo
 
Understanding the New BP Deepwater Horizon Settlement
Understanding the New BP Deepwater Horizon SettlementUnderstanding the New BP Deepwater Horizon Settlement
Understanding the New BP Deepwater Horizon Settlementlijoam
 
Babatunde Mobisola - Accumulator Systems
Babatunde Mobisola - Accumulator  SystemsBabatunde Mobisola - Accumulator  Systems
Babatunde Mobisola - Accumulator SystemsMobisola Babatunde
 
Macondo Feedback Event
Macondo Feedback EventMacondo Feedback Event
Macondo Feedback EventMatthew Lowe
 
Environmental Response Management Application (ERMA): From Portsmouth Respons...
Environmental Response Management Application (ERMA): From Portsmouth Respons...Environmental Response Management Application (ERMA): From Portsmouth Respons...
Environmental Response Management Application (ERMA): From Portsmouth Respons...Kurt Schwehr
 
Mashables take on bp oil
Mashables take on bp oilMashables take on bp oil
Mashables take on bp oilsabeu
 
63 Profit Loss
63 Profit Loss63 Profit Loss
63 Profit LossPAVO
 
3.3 balance sheets
3.3 balance sheets3.3 balance sheets
3.3 balance sheetssdwaltton
 

Destacado (20)

Deep Water Horizon Accident Investigation Lessons Learned
Deep Water Horizon Accident Investigation Lessons LearnedDeep Water Horizon Accident Investigation Lessons Learned
Deep Water Horizon Accident Investigation Lessons Learned
 
Deepwater Horizon Oil Spill
Deepwater Horizon Oil SpillDeepwater Horizon Oil Spill
Deepwater Horizon Oil Spill
 
BP's Deepwater Oil Spill Case Study Analysis - Business Ethics
BP's Deepwater Oil Spill Case Study Analysis - Business EthicsBP's Deepwater Oil Spill Case Study Analysis - Business Ethics
BP's Deepwater Oil Spill Case Study Analysis - Business Ethics
 
Deepwater horizon revisited investigative insights
Deepwater horizon revisited   investigative insightsDeepwater horizon revisited   investigative insights
Deepwater horizon revisited investigative insights
 
Deepwater horizon
Deepwater horizonDeepwater horizon
Deepwater horizon
 
Piper alpha
Piper alphaPiper alpha
Piper alpha
 
Deepwater Horizon Oil Spill: A Study of Behavioural Decision Making
Deepwater Horizon Oil Spill: A Study of Behavioural Decision MakingDeepwater Horizon Oil Spill: A Study of Behavioural Decision Making
Deepwater Horizon Oil Spill: A Study of Behavioural Decision Making
 
Operational Discipline - Deepwater Horizon Case Study
Operational Discipline - Deepwater Horizon Case StudyOperational Discipline - Deepwater Horizon Case Study
Operational Discipline - Deepwater Horizon Case Study
 
DAVOS GRF5 TSIG DEEPWATER HORIZON
DAVOS GRF5 TSIG DEEPWATER HORIZONDAVOS GRF5 TSIG DEEPWATER HORIZON
DAVOS GRF5 TSIG DEEPWATER HORIZON
 
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...
Changes to federal offshore drilling regulation after Deepwater Horizon (Dec ...
 
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBA
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBABP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBA
BP Deepwater Horizon oil spill's impact on the us economy, Jonah Guo,Queen's MBA
 
Understanding the New BP Deepwater Horizon Settlement
Understanding the New BP Deepwater Horizon SettlementUnderstanding the New BP Deepwater Horizon Settlement
Understanding the New BP Deepwater Horizon Settlement
 
Babatunde Mobisola - Accumulator Systems
Babatunde Mobisola - Accumulator  SystemsBabatunde Mobisola - Accumulator  Systems
Babatunde Mobisola - Accumulator Systems
 
BP's oil spill desaster
BP's oil spill desasterBP's oil spill desaster
BP's oil spill desaster
 
Macondo Feedback Event
Macondo Feedback EventMacondo Feedback Event
Macondo Feedback Event
 
Environmental Response Management Application (ERMA): From Portsmouth Respons...
Environmental Response Management Application (ERMA): From Portsmouth Respons...Environmental Response Management Application (ERMA): From Portsmouth Respons...
Environmental Response Management Application (ERMA): From Portsmouth Respons...
 
Food chain
Food chainFood chain
Food chain
 
Mashables take on bp oil
Mashables take on bp oilMashables take on bp oil
Mashables take on bp oil
 
63 Profit Loss
63 Profit Loss63 Profit Loss
63 Profit Loss
 
3.3 balance sheets
3.3 balance sheets3.3 balance sheets
3.3 balance sheets
 

Similar a Deepwater horizon accident_investigation_static_presentation

Chairul abdi's technical paper
Chairul abdi's technical paperChairul abdi's technical paper
Chairul abdi's technical paperChairul Abdi
 
Well completion.
Well completion.Well completion.
Well completion.Mawa James
 
WBM & OBM Drilling Fluids.pptx
WBM & OBM Drilling Fluids.pptxWBM & OBM Drilling Fluids.pptx
WBM & OBM Drilling Fluids.pptxAihamAltayeh1
 
CFA and DD Piles in Earthquake Country - DM Holloway - SEAOSC Seminar - Long...
CFA and DD Piles in Earthquake Country  - DM Holloway - SEAOSC Seminar - Long...CFA and DD Piles in Earthquake Country  - DM Holloway - SEAOSC Seminar - Long...
CFA and DD Piles in Earthquake Country - DM Holloway - SEAOSC Seminar - Long...Dan Brown and Associates, PC
 
Water shut off ppt
Water shut off pptWater shut off ppt
Water shut off pptAdjei Sephen
 

Similar a Deepwater horizon accident_investigation_static_presentation (7)

TCD2011 - Kunne bedre kompetanse avverget Macondo-ulykken i Mexico-gulfen? v/...
TCD2011 - Kunne bedre kompetanse avverget Macondo-ulykken i Mexico-gulfen? v/...TCD2011 - Kunne bedre kompetanse avverget Macondo-ulykken i Mexico-gulfen? v/...
TCD2011 - Kunne bedre kompetanse avverget Macondo-ulykken i Mexico-gulfen? v/...
 
Chairul abdi's technical paper
Chairul abdi's technical paperChairul abdi's technical paper
Chairul abdi's technical paper
 
Well completion.
Well completion.Well completion.
Well completion.
 
WBM & OBM Drilling Fluids.pptx
WBM & OBM Drilling Fluids.pptxWBM & OBM Drilling Fluids.pptx
WBM & OBM Drilling Fluids.pptx
 
CFA and DD Piles in Earthquake Country - DM Holloway - SEAOSC Seminar - Long...
CFA and DD Piles in Earthquake Country  - DM Holloway - SEAOSC Seminar - Long...CFA and DD Piles in Earthquake Country  - DM Holloway - SEAOSC Seminar - Long...
CFA and DD Piles in Earthquake Country - DM Holloway - SEAOSC Seminar - Long...
 
Water shut off ppt
Water shut off pptWater shut off ppt
Water shut off ppt
 
MANAGING A GOLD MINE TAILINGS DAM
MANAGING A GOLD MINE TAILINGS DAMMANAGING A GOLD MINE TAILINGS DAM
MANAGING A GOLD MINE TAILINGS DAM
 

Último

Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptx
Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptxContemporary Economic Issues Facing the Filipino Entrepreneur (1).pptx
Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptxMarkAnthonyAurellano
 
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...lizamodels9
 
8447779800, Low rate Call girls in Tughlakabad Delhi NCR
8447779800, Low rate Call girls in Tughlakabad Delhi NCR8447779800, Low rate Call girls in Tughlakabad Delhi NCR
8447779800, Low rate Call girls in Tughlakabad Delhi NCRashishs7044
 
8447779800, Low rate Call girls in Saket Delhi NCR
8447779800, Low rate Call girls in Saket Delhi NCR8447779800, Low rate Call girls in Saket Delhi NCR
8447779800, Low rate Call girls in Saket Delhi NCRashishs7044
 
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...lizamodels9
 
Future Of Sample Report 2024 | Redacted Version
Future Of Sample Report 2024 | Redacted VersionFuture Of Sample Report 2024 | Redacted Version
Future Of Sample Report 2024 | Redacted VersionMintel Group
 
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In.../:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...lizamodels9
 
International Business Environments and Operations 16th Global Edition test b...
International Business Environments and Operations 16th Global Edition test b...International Business Environments and Operations 16th Global Edition test b...
International Business Environments and Operations 16th Global Edition test b...ssuserf63bd7
 
Case study on tata clothing brand zudio in detail
Case study on tata clothing brand zudio in detailCase study on tata clothing brand zudio in detail
Case study on tata clothing brand zudio in detailAriel592675
 
Kenya’s Coconut Value Chain by Gatsby Africa
Kenya’s Coconut Value Chain by Gatsby AfricaKenya’s Coconut Value Chain by Gatsby Africa
Kenya’s Coconut Value Chain by Gatsby Africaictsugar
 
Innovation Conference 5th March 2024.pdf
Innovation Conference 5th March 2024.pdfInnovation Conference 5th March 2024.pdf
Innovation Conference 5th March 2024.pdfrichard876048
 
Global Scenario On Sustainable and Resilient Coconut Industry by Dr. Jelfina...
Global Scenario On Sustainable  and Resilient Coconut Industry by Dr. Jelfina...Global Scenario On Sustainable  and Resilient Coconut Industry by Dr. Jelfina...
Global Scenario On Sustainable and Resilient Coconut Industry by Dr. Jelfina...ictsugar
 
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...lizamodels9
 
Digital Transformation in the PLM domain - distrib.pdf
Digital Transformation in the PLM domain - distrib.pdfDigital Transformation in the PLM domain - distrib.pdf
Digital Transformation in the PLM domain - distrib.pdfJos Voskuil
 
The CMO Survey - Highlights and Insights Report - Spring 2024
The CMO Survey - Highlights and Insights Report - Spring 2024The CMO Survey - Highlights and Insights Report - Spring 2024
The CMO Survey - Highlights and Insights Report - Spring 2024christinemoorman
 
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...lizamodels9
 
MAHA Global and IPR: Do Actions Speak Louder Than Words?
MAHA Global and IPR: Do Actions Speak Louder Than Words?MAHA Global and IPR: Do Actions Speak Louder Than Words?
MAHA Global and IPR: Do Actions Speak Louder Than Words?Olivia Kresic
 
2024 Numerator Consumer Study of Cannabis Usage
2024 Numerator Consumer Study of Cannabis Usage2024 Numerator Consumer Study of Cannabis Usage
2024 Numerator Consumer Study of Cannabis UsageNeil Kimberley
 
Market Sizes Sample Report - 2024 Edition
Market Sizes Sample Report - 2024 EditionMarket Sizes Sample Report - 2024 Edition
Market Sizes Sample Report - 2024 EditionMintel Group
 
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCRashishs7044
 

Último (20)

Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptx
Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptxContemporary Economic Issues Facing the Filipino Entrepreneur (1).pptx
Contemporary Economic Issues Facing the Filipino Entrepreneur (1).pptx
 
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
 
8447779800, Low rate Call girls in Tughlakabad Delhi NCR
8447779800, Low rate Call girls in Tughlakabad Delhi NCR8447779800, Low rate Call girls in Tughlakabad Delhi NCR
8447779800, Low rate Call girls in Tughlakabad Delhi NCR
 
8447779800, Low rate Call girls in Saket Delhi NCR
8447779800, Low rate Call girls in Saket Delhi NCR8447779800, Low rate Call girls in Saket Delhi NCR
8447779800, Low rate Call girls in Saket Delhi NCR
 
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...
Lowrate Call Girls In Sector 18 Noida ❤️8860477959 Escorts 100% Genuine Servi...
 
Future Of Sample Report 2024 | Redacted Version
Future Of Sample Report 2024 | Redacted VersionFuture Of Sample Report 2024 | Redacted Version
Future Of Sample Report 2024 | Redacted Version
 
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In.../:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...
/:Call Girls In Indirapuram Ghaziabad ➥9990211544 Independent Best Escorts In...
 
International Business Environments and Operations 16th Global Edition test b...
International Business Environments and Operations 16th Global Edition test b...International Business Environments and Operations 16th Global Edition test b...
International Business Environments and Operations 16th Global Edition test b...
 
Case study on tata clothing brand zudio in detail
Case study on tata clothing brand zudio in detailCase study on tata clothing brand zudio in detail
Case study on tata clothing brand zudio in detail
 
Kenya’s Coconut Value Chain by Gatsby Africa
Kenya’s Coconut Value Chain by Gatsby AfricaKenya’s Coconut Value Chain by Gatsby Africa
Kenya’s Coconut Value Chain by Gatsby Africa
 
Innovation Conference 5th March 2024.pdf
Innovation Conference 5th March 2024.pdfInnovation Conference 5th March 2024.pdf
Innovation Conference 5th March 2024.pdf
 
Global Scenario On Sustainable and Resilient Coconut Industry by Dr. Jelfina...
Global Scenario On Sustainable  and Resilient Coconut Industry by Dr. Jelfina...Global Scenario On Sustainable  and Resilient Coconut Industry by Dr. Jelfina...
Global Scenario On Sustainable and Resilient Coconut Industry by Dr. Jelfina...
 
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
Call Girls In Sikandarpur Gurgaon ❤️8860477959_Russian 100% Genuine Escorts I...
 
Digital Transformation in the PLM domain - distrib.pdf
Digital Transformation in the PLM domain - distrib.pdfDigital Transformation in the PLM domain - distrib.pdf
Digital Transformation in the PLM domain - distrib.pdf
 
The CMO Survey - Highlights and Insights Report - Spring 2024
The CMO Survey - Highlights and Insights Report - Spring 2024The CMO Survey - Highlights and Insights Report - Spring 2024
The CMO Survey - Highlights and Insights Report - Spring 2024
 
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...
Call Girls In Connaught Place Delhi ❤️88604**77959_Russian 100% Genuine Escor...
 
MAHA Global and IPR: Do Actions Speak Louder Than Words?
MAHA Global and IPR: Do Actions Speak Louder Than Words?MAHA Global and IPR: Do Actions Speak Louder Than Words?
MAHA Global and IPR: Do Actions Speak Louder Than Words?
 
2024 Numerator Consumer Study of Cannabis Usage
2024 Numerator Consumer Study of Cannabis Usage2024 Numerator Consumer Study of Cannabis Usage
2024 Numerator Consumer Study of Cannabis Usage
 
Market Sizes Sample Report - 2024 Edition
Market Sizes Sample Report - 2024 EditionMarket Sizes Sample Report - 2024 Edition
Market Sizes Sample Report - 2024 Edition
 
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR
8447779800, Low rate Call girls in Kotla Mubarakpur Delhi NCR
 

Deepwater horizon accident_investigation_static_presentation

  • 1. Deepwater Horizon Investigation Deepwater Horizon Accident Investigation 1
  • 2. Investigation Context Terms of Reference Investigation Team Data and Analysis Investigation Limitations Deepwater Horizon Accident Investigation 2
  • 3. Eight Barriers Were Breached Well integrity was not established or failed 6 7 − Annulus cement barrier did not isolate hydrocarbons 1 3 5 − Shoe track barriers did not isolate hydrocarbons 2 Hydrocarbons entered the well undetected and Riser 4 well control was lost − Negative pressure test was accepted although well 3 8 integrity had not been established BOP Sea Floor − Influx was not recognized until hydrocarbons were in 4 riser − Well control response actions failed to regain control of 5 Casing well Hydrocarbons ignited on the Deepwater Horizon − Diversion to mud gas separator resulted in gas venting 6 onto rig − Fire and gas system did not prevent hydrocarbon 7 ignition Blowout preventer did not seal the well 1 Reservoir − Blowout preventer (BOP) emergency mode did not 8 seal well 2 Deepwater Horizon Accident Investigation 3
  • 4. Introduction Technical Presentation Deepwater Horizon Accident Investigation 4
  • 5. Well Integrity Was Not Established or Failed Deepwater Horizon Accident Investigation 5
  • 6. Production Casing Installation After drilling to total depth, casing is run to bottom in preparation for the cement job. A Choke double valve float collar is used to prevent Kill Boost backflow or ingress of fluids through the shoe track until the cement hardens and creates a permanent barrier. BOP April 18th 00:30 – April 19th 19:30 Sea Floor 17:30 – 19:30 Long string design robust, consistent with Circulated prior Cement 36” to cement job similar wells in the area Mud 9 attempts made to establish circulation 28” Spacer to convert float valves 22” Circulate ~6 times open hole volume, 18” limited circulation due to concerns over 16” creating losses and hole washout 13-5/8” No evidence that hydrocarbons entered 11-7/8” the wellbore prior to the cementing 9-7/8” operation 14.17 ppg SOBM Primary reservoir sands (12.6 ppg) Bottoms–up Marker Deepwater Horizon Accident Investigation 6
  • 7. Cement Job Cement is pumped down casing through the float collar and up the annulus to isolate the primary reservoir sands. Choke Pull out of hole Kill April 19th 19:30 – April 20th 07:00 Boost with running tool and drill Nitrogen cement slurry chosen pipe – To achieve light weight slurry due to BOP Set and test limited pore pressure / fracture casing hanger seal assembly gradient window Sea Floor 00:35 – 02:50 Possible risk 36” Drill-Quip seal assembly installed – Stability of foam Base Oil and successfully tested. Centralizer No lock down sleeve installed. – Relatively small volume Spacer 28” 02:50 – 07:00 – Susceptible to contamination Cap Pull out hole with drill pipe. Cement 22” Mitigation of risk by Foamed 18” – Thorough testing of slurry design Cement Bottoms–up 16” Marker – Precise placement Tail Cement Mud 13-5/8” Centralization Primary Nitrogen 11-7/8” Reservoir – 6 inline centralizers spaced across Breakout Sands the reservoir sands Shoe – 17,168’ (12.6 ppg) Top of 9-7/8” cement 17,260’ – Additional centralizers not run because incorrectly thought to be wrong type Primary reservoir Float Collar – 18,115’ 6 centralizers sands – Risk of channeling above reservoir (12.6 ppg) sands known and accepted Shoe – 18,304’ Deepwater Horizon Accident Investigation 7
  • 8. Key Finding #1 The annulus cement barrier did not isolate the reservoir hydrocarbons Cement is pumped down the Cement Slurry Placement landing string and casing into the Base Oil ppg 16.7ppg 6.7 annulus to isolate hydrocarbon bearing sands. Spacer 14.3 ppg Riser 14.3 ppg Cap Cement Mud Channeling 16.74 ppg Foam slurry recommended was a 14.17 ppg Cap Cement complex design 16.74 ppg BOP Risk of contamination using small Sea Floor Foam volume of cement Cement Foam 14.5 ppg Cement No fluid loss additives 14.5 ppg Incomplete pre-job cement lab Casing Centralizers Spacer testing 14.3 ppg Foam slurry was likely unstable Float Collar Top Wiper Plug Top Wiper Plug and resulted in nitrogen breakout Bottom Wiper Plug Bottom Wiper Plug Shoe Tail Cement Track 16.74 ppg 12.6 ppg Shoe Track Reservoir Reamer Shoe Tail Cement Nitrogen Breakout Deepwater Horizon Accident Investigation 8
  • 9. Cement Slurry Design Issues An independent lab completed over 500 tests on a representative cement slurry and reported the following: 50% quality foam at surface conditions Original Height was not stable 18.5% quality foam (downhole quality) was not stable Yield point of the Halliburton slurry was too low for the foam cement (2 lb / 100 ft2 Final Height yield point at 135 deg F) Fluid loss for the base slurry was excessive compared to industry recommendations (302 cc versus 50 cc per 30 min) Cement Note: QUALITY = Nitrogen Volume / (Nitrogen + Base Slurry Volume) Unstable Foam Sample Deepwater Horizon Accident Investigation 9
  • 10. Flow Through Shoe Track - Supporting Evidence Casing Key Observations for Flow Seal Shoe Through Shoe vs. Seal Assembly Failure Assembly Failure Y Mechanical Barrier Failure Mode Identified Y Y Realistic Net Pay Assumption N Y 1400 psi recorded on drill pipe during negative N test at 18:30 Y Ability to flow from 20:58 N Y Pressure Increase from 21:08 to 21:14 N 16ppg Spacer Y Pressure Response from 21:31 to 21:34 N 14.17ppg SOBM (Mud) 8.6ppg Seawater Influx Y Timing for Gas Arrival to Surface N Seal N Casing Static Kill Shoe Failure Y Assembly Failure Deepwater Horizon Accident Investigation 10
  • 11. Key Finding #2 The shoe track mechanical barriers did not isolate the hydrocarbons Tail cement is displaced down the casing into the shoe track. The tail cement is designed to prevent flow from the annulus into the casing. The float collar valves, which provide a second barrier, Riser must close and seal to prevent flow up Hydrocarbon Flow the casing. Path Shoe track had two types of mechanical BOP Float Collar barriers: cement in the shoe track and the Sea Floor double check valves in the float collar Shoe track cement failed to act as a Check Valves Casing barrier due to contamination of the base slurry by break out of nitrogen from the foam slurry Shoe track cement Hydrocarbon influx was able to bypass the float collar check valves due to either: Valves failed to convert or Valves failed to seal Centralizers Flow through shoe confirmed by fluid modeling and Macondo static kill data Reservoir Flow Ports Deepwater Horizon Accident Investigation 11
  • 12. Hydrocarbons Entered the Well Undetected and Well Control Was Lost Deepwater Horizon Accident Investigation 12
  • 13. Casing (Positive) Pressure Test 2700 psi Kill A positive pressure test verifies the integrity of the casing and seal assembly. April 20th 07:00 – 12:00 Sea Floor Casing was pressure tested to: Cement 250 psi (low) Mud 2700 psi (high) Spacer Test successful Proved integrity of blind shear rams, seal assembly, casing and wiper plug Test does not test the shoe track due to presence of wiper plug Primary reservoir sands Deepwater Horizon Accident Investigation 13
  • 14. Negative Pressure Test The negative-pressure test checks the integrity of the shoe track, casing and wellhead seal assembly. This simulates Choke Boost Kill 15:04 – 15:56 conditions during temporary Seawater pumped into abandonment when a portion of the well Boost, Choke, and Kill lines is displaced to seawater. BOP April 20th 15:04 – 19:55 16:54 - Close Annular Sea Floor Negative test simulates underbalanced 15:56 – 16:53 424 bbls of 16 ppg condition spacer followed by 30 bbls Cement of freshwater and 352 bbls Spacer used between mud and seawater of seawater pumped into well Mud Leaking annular at start of test moved Spacer 16:54 – 16:59 spacer across kill line inlet 50 bbls bled off Seawater drill pipe due to Negative test started on drill pipe but Influx leaking annular changed to kill line Bleed volumes higher than calculated Drill pipe built pressure to 1400 psi with no flow on the kill line Primary reservoir sands (12.6 ppg) Deepwater Horizon Accident Investigation 14
  • 15. Negative Pressure Test The negative-pressure test checks the 17:52 – 18:00 integrity of the shoe track, casing and Open kill line to conduct wellhead seal assembly. This simulates Choke negative test Kill conditions during temporary Boost 16:59 – 17:08 abandonment when a portion of the well Bled 3 - 15 bbls into kill line Annular seals with is displaced to seawater. increased hydraulic BOP closing pressure Flow did not April 20th 15:04 – 19:55 stop and Fill riser with 50 bbls of mud “spurted” Negative test simulates underbalanced Sea Floor Kill line closed 17:08 – 17:27 condition Monitored that the Cement annular sealed Spacer used between mud and seawater Mud 17:27 Leaking annular at start of test moved Bled 15 bbls of spacer across kill line inlet Spacer seawater from drill pipe Seawater Negative test started on drill pipe but Decision made to Influx change test to kill line changed to kill line Bleed volumes higher than calculated Cement Tank Total Drill pipe built pressure to 1400 psi with Volume no flow on the kill line 15 bbls Primary reservoir sands (12.6 ppg) Deepwater Horizon Accident Investigation 15
  • 16. Negative Pressure Test The negative-pressure test checks the 1400 0 integrity of the shoe track, casing and psi psi 18:00 – 18:35 wellhead seal assembly. This simulates Choke Drill pipe pressure gradually Boost increased to 1400 psi conditions during temporary abandonment when a portion of the well 18:42 is displaced to seawater. BOP Pumped into kill line to confirm full April 20th 15:04 – 19:55 Kill line opened for Sea Floor monitoring negative test Negative test simulates underbalanced condition Cement 18:42 – 19:55 Spacer used between mud and seawater Monitored kill line for 30 min Mud 1400 psi on drill pipe described Leaking annular at start of test moved as a “bladder effect” spacer across kill line inlet Spacer Seawater 19:55 Negative pressure test Negative test started on drill pipe but Influx was concluded and changed to kill line considered a good test Bleed volumes higher than calculated Cement Tank Total Drill pipe built pressure to 1400 psi with Volume no flow on the kill line 18 bbls Additional 15 bbls 3 bbl influx Primary reservoir sands (12.6 ppg) Deepwater Horizon Accident Investigation 16
  • 17. Key Finding #3 The negative pressure test was accepted although well integrity had not been established 1400 0 PSI PSI Riser Choke Kill Bleed volumes not recognized as a Boost problem BOP Sea Floor BOP Anomalous pressure on drill pipe with no Sea Floor flow from kill line Spacer Casing SOBM Test incorrectly accepted as successful Spacer Seawater Negative testing not standardized Influx Shoe – 17,168’ TOC – 17,260’ FC – 18,115’ Reservoir Shoe – 18,304’ Deepwater Horizon Accident Investigation 17
  • 18. Well Monitoring – Driller’s Console and Mudlogging unit Well monitoring is performed to understand if the well has losses or gains Driller is responsible for monitoring and shutting in the well The mudlogger provides monitoring support to the driller Displays and trending capability available in both Driller’s and Mudlogger’s cabins Flow, pressure and pit sensors can indicate flow Simultaneous activities were taking place on April 20th to prepare for rig move Standards for monitoring do not specifically address end-of-well activities Deepwater Horizon Accident Investigation 18
  • 19. Undetected Flowing Conditions Mud in the riser is displaced with seawater in preparation for temporary abandonment. Choke Kill Boost 21:08 Spacer arrived at surface April 20th 19:55 – 21:14 Shut pumps down for sheen test BOP 20:02 Resume displacement of mud with 20:02 seawater Sea Floor Annular opened after negative test 20:52 Well becomes underbalanced and starts to flow Cement 20:00 – 21:08 Resumed pumping Mud Displaced riser with seawater After 20:58 gain being taken and pressure Spacer until spacer is at surface begins increasing Seawater 20:52 – Flow from well masked by emptying Mud + Seawater Well becomes underbalanced of trip tank Mix Influx 21:08 Pumping stops for sheen test – Pressure increases with pump off 20:58 - 21:08 39 bbl gain 21:14 Sheen test complete, displacement resumes Primary reservoir sands (12.6 ppg) Deepwater Horizon Accident Investigation 19
  • 20. Key Finding #4 The influx was not recognized until hydrocarbons were in the riser 2000 3000 Flow Indications Based on Real-time Data Flow indications: Flow Out (calibrated) 1800 Flow In (rig pumps) DP Press (rig pumps) 2500 #1: Drill pipe pressure 1600 increased by 100 psi, Decreasing trend should 1400 (expected decreased); Pump Pressure (psi) have continued 2000 ~39 bbl gain from 20:58 Flow Rate (gpm) 1200 Indication #1 to 21:08 1000 1500 800 1000 600 400 20:52-Flow starts 500 200 Cumulative Gain 0 0 39 300 0 bbl bbl bbl 20:45 20:50 20:55 21:00 21:05 21:10 21:15 21:20 21:25 21:30 21:35 1,017 psi SOBM (mud) Seawater Influx SOBM + seawater mix 21:08 Deepwater Horizon Accident Investigation 20
  • 21. Key Finding #4 The influx was not recognized until hydrocarbons were in the riser 2000 3000 Flow Indications Based on Real-time Data Flow indications: Flow Out (calibrated) 1800 Flow In (rig pumps) DP Press (rig pumps) 2500 #1: Drill pipe pressure 1600 increased by 100 psi, Decreasing trend should 1400 (expected decreased); Pump Pressure (psi) have continued 2000 ~39 bbl gain from 20:58 Flow Rate (gpm) 1200 Indication #1 to 21:08 1000 1500 800 #2: Drill pipe pressure Indication #2 increased by 246 psi with 1000 600 Overboard line opened pumps off 400 20:52-Flow starts Flow out available only 500 to driller after 21:10 – Flow out does not 200 immediately drop Cumulative Gain 0 39 300 0 bbl bbl bbl 0 after shutting down 20:45 20:50 20:55 21:00 21:05 21:10 21:15 21:20 21:25 21:30 21:35 pump 1,017 psi 1200 Normal Flow Back 1000 Flow Out Flow Rate (gpm) Flow In 800 SOBM (mud) Seawater 600 Influx SOBM + seawater mix 400 200 21:08 0 16:50 16:55 17:00 17:05 Deepwater Horizon Accident Investigation 21
  • 22. Key Finding #4 The influx was not recognized until hydrocarbons were in the riser 2000 3000 Flow Indications Based on Real-time Data Flow indications: Flow Out (calibrated) 1800 Flow In (rig pumps) DP Press (rig pumps) 2500 #1: Drill pipe pressure 1600 increased by 100 psi, 1400 Indication #3 (expected decreased); Pump Pressure (psi) 2000 ~39 bbl gain from 20:58 Flow Rate (gpm) 1200 Indication #1 to 21:08 1000 1500 800 #2: Drill pipe pressure Indication #2 increased by 246 psi with 1000 600 pumps off 400 20:52-Flow starts 500 – Flow out does not 200 immediately drop Cumulative Gain 0 39 300 0 bbl bbl bbl 0 after shutting down 20:45 20:50 20:55 21:00 21:05 21:10 21:15 21:20 21:25 21:30 21:35 pump 1,017 psi 1,200 psi #3: Drill pipe pressure increased by 556 psi with pumps off; ~300 bbl gain SOBM (mud) Seawater No well control actions taken Influx SOBM + seawater mix 21:08 21:31 Deepwater Horizon Accident Investigation 22
  • 23. Key Finding #5 Well control response actions failed to regain control of the well Influx enters riser 3000 Based on Real-time Data First indication of well control response: 49 minutes and 1000 bbls after initial influx Drill Pipe Presssure (psi) 2500 BOP Mud shoots up derrick Attempt to bleed -Diverter closed pressure -BOP activated 2000 Explosion at 21:49 Close Drill Pipe BOP Sealing 1500 Annular Discussion about leaking 1000 “Differential Pressure” - Mud and water raining onto deck Mud overflowing onto rig floor - TP calls WSL, getting mud back, 500 diverted to MGS, closed or was Pumps shut down closing annular Pressure increase due - AD calls Senior TP, Well blowing 0 to annular activation out, TP is shutting it in now 21:30 21:32 21:34 21:36 21:38 21:40 21:42 21:44 21:46 21:48 21:50 Deepwater Horizon Accident Investigation 23
  • 24. Hydrocarbons Ignited on the Deepwater Horizon Deepwater Horizon Accident Investigation 24
  • 25. Diverting to the Mud Gas Separator at about 21:42 12” Vent When responding to a well control event the riser diverter is closed and fluids 6” Vacuum Breaker sent to either the mud gas separator or Bursting Disk to the overboard diverter lines. Diversion to the MGS MGS Rated to 60 psi working pressure Rig crew has the option to divert flow to Rotary Hose Mud port/starboard overboard lines or the System IBOP MGS Starboard Diverter Overboard Diverting to port or starboard will result in Starboard fluids venting overboard Port Overboard 14” Diverter Line 14” Diverter Line Overboard Slip Joint Rated to 100 or 500 psi Liquid outlet from MGS goes to the Mud Overboard Caisson Boost Kill System under the main deck Choke BOP Seawater Seawater/Mud Mix Influx Deepwater Horizon Accident Investigation 25
  • 26. Gas flow to Surface at high rate: 21:46 to 22:00 12” Vent When responding to a well control event the riser diverter is closed and fluids 6” Vacuum Breaker sent to either the mud gas separator or Bursting Disk to the overboard diverter lines. Hydrocarbon flow from surface MGS equipment Rotary Hose Mud Instantaneous gas rates reached System IBOP 165 mmscfd Starboard Diverter Overboard Pressures exceeded operating ratings (above 100 psi) Port Starboard Overboard 14” Diverter Line 14” Diverter Line Overboard Gas would probably have vented from: Slip Joint Overboard Caisson Boost Kill Slip joint packer into the moon pool Choke 12” MGS “gooseneck” vent BOP 6” MGS vacuum breaker vent 6” overboard line through burst disk Seawater 10” mud line under the main deck Seawater/Mud Mix Influx Deepwater Horizon Accident Investigation 26
  • 27. Gas Dispersion across the Deepwater Horizon 21:46 to 21:50 hrs Animation of Gas Dispersion Upper Explosive Limit Lower Explosive Limit 3D View Cut Section Through Derrick Towards Aft Deepwater Horizon Accident Investigation 27
  • 28. Secondary protective systems did not prevent ignition Secondary protective systems are designed to reduce the potential consequence of an event once the 3D view primary protective systems have failed. Fwd Aft Secondary Protective Systems Gas cloud reached the supply air intakes for engine rooms 3, 4, 5 & 6 The Fire and Gas system did not automatically trigger a shutdown of the HVAC system for the engine rooms Limited areas of the rig are designated as electrically classified zones Deepwater Horizon Accident Investigation 28
  • 29. Key Finding #6 Diversion to the mud gas separator resulted in gas venting onto the 12” Vent rig 6” Vacuum Breaker When responding to a well control event Bursting Disk the riser diverter is closed and fluids are sent to either the mud gas separator or to the overboard diverter lines. MGS Rotary Hose Hydrocarbons were routed to the mud gas Mud System IBOP separator instead of diverting overboard Starboard Resulted in rapid gas dispersion across Diverter Overboard the rig through the MGS vents and mud system Port Starboard Overboard 14” Diverter Line 14” Diverter Line Overboard Slip Joint Overboard Caisson Boost Kill Choke BOP BOP Sealed at Seawater 21:47 Seawater/Mud Mix Influx Deepwater Horizon Accident Investigation 29
  • 30. Key Finding #7 The fire and gas system did not prevent hydrocarbon ignition Gas Dispersion at 4 minutes Secondary protective systems are designed to reduce the potential (Upper Explosive Limit) consequence of an event once the primary protective systems have Aft failed. Gas dispersion beyond electrically classified areas Section through derrick 3D view Gas ingress into engine rooms via main (Lower Explosive Limit) Fwd deck air intakes The on-line engines were one potential source of ignition Fwd 3D view Aft Aft Deepwater Horizon Accident Investigation 30
  • 31. Emergency Well Control System Did Not Seal the Well Deepwater Horizon Accident Investigation 31
  • 32. Blowout Preventer (BOP) BOP Control Panel Surface HPU & Accumulators Flex Joint LMRP Upper Annular Lower Annular Stripping Element Mux Cable Hydraulic Conduit LMRP Accumulators Blind Shear Ram Blue Yellow Control Control Casing Shear Ram Pod Pod (Non Sealing) Upper VBR Lower Stack Middle VBR Accumulators Lower (Test) VBR BOP Stack Emergency Methods of BOP Operation Available on DW Horizon Wellhead Connector Manual Automatic ROV Intervention Wellhead HOT Stab EDS AMF AMF Sea Bed HP BSR Close Auto-shear Deepwater Horizon Accident Investigation 32
  • 33. BOP Response (Before the Explosions) BOP is designed to seal the wellbore and 20th April shear casing or drill pipe if necessary. 21:38 – Hydrocarbons enter the riser April 20th 21:41 annular BOP closed but appears Activation of Upper Annular Lower Annular BOP not to have sealed the annulus Lower Annular 21:47 a VBR likely closed and sealed the Stripping Element annulus Blind Shear Ram Casing Shear Ram Activation of VBR (Non Sealing) Upper VBR Middle VBR Lower (Test) VBR Wellhead Connector Wellhead Sea Bed Deepwater Horizon Accident Investigation 33
  • 34. BOP Response (Impact of Explosions) MUX cables provide electronic communication and electrical power to the BOP control pods. April 20th Damage to MUX cables and hydraulic line Upper Annular – Opening of annular BOP Lower Annular Annular BOP Stripping Element gradually opens Rig drifted off location – Upward movement of the drill pipe in the BOP Blind Shear Ram Casing Shear Ram (Non Sealing) Upper VBR Middle VBR Lower (Test) VBR Wellhead Connector Wellhead Sea Bed Deepwater Horizon Accident Investigation 34
  • 35. BOP Response (After the Explosions) There are several emergency methods of activating the BSR to seal the well. April 20th EDS attempts failed to activate BSR Upper Annular AMF sequence likely failed to activate BSR Lower Annular April 21st – 22nd Stripping Element BSR activated by ROV hot stab attempts to close BOP were Auto-shear ineffective ROV simulated AMF function likely failed to Blind Shear Ram activate BSR Casing Shear Ram (Non Sealing) ROV activated auto-shear appears to have Upper VBR activated but did not seal the well Middle VBR April 25th – May 5th Lower (Test) VBR Further ROV attempts using seabed deployed accumulators were unsuccessful Wellhead Connector Wellhead Sea Bed Deepwater Horizon Accident Investigation 35
  • 36. Key Finding #8 The BOP emergency mode did not seal the well Explosions & Fire: The AMF provides an automatic Loss of communication means of closing the BSR without Loss of electrical power crew intervention. Loss of hydraulics EDS function was inoperable due to Damaged Hydraulic Conduit damage to MUX cables Damaged MUX Cable AMF could not activate the BSR due to defects in both control pods Auto-shear appears to have activated Blue Yellow the BSR but did not seal the well Control Control Pod Pod Potential weaknesses found in the BOP testing regime and maintenance management systems Emergency Methods of BOP Operation Available on DW Horizon Manual Automatic ROV Intervention HOT Stab EDS AMF AMF HP BSR Close Auto-shear Deepwater Horizon Accident Investigation 36
  • 37. Summary of Findings and Recommendations Deepwater Horizon Accident Investigation 37
  • 38. Recommendations 25 Recommendations Specific to the 8 Key Findings BP Drilling Operating Practice and Management Systems Engineering Technical Practices and Procedures Further Enhance Deepwater Capability and Proficiency Strengthen Rig Audit Action Closeout and Verification Introduce Integrity Performance Management for Drilling and Wells Activities Contractor and Service Provider Oversight and Assurance Cementing Services Drilling Contractor Well Control Practices and Proficiency Oversight of Rig Safety Critical Equipment BOP Configuration and Capability BOP Minimum Criteria for Testing, Maintenance, System Modifications and Performance Reliability BP has accepted all the recommendations and is reviewing how best to implement across its world wide operations Deepwater Horizon Accident Investigation 38
  • 39. Summary of Key Findings Well integrity was not established or failed 6 7 − Annulus cement barrier did not isolate hydrocarbons 1 3 5 − Shoe track barriers did not isolate hydrocarbons 2 Hydrocarbons entered the well undetected and Riser 4 well control was lost − Negative pressure test was accepted although well 3 8 integrity had not been established BOP Sea Floor − Influx was not recognized until hydrocarbons were in 4 riser − Well control response actions failed to regain control of 5 Casing well Hydrocarbons ignited on the Deepwater Horizon − Diversion to mud gas separator resulted in gas venting 6 onto rig − Fire and gas system did not prevent hydrocarbon 7 ignition Blowout preventer did not seal the well 1 Reservoir − Blowout preventer (BOP) emergency modes did not 8 seal well 2 Deepwater Horizon Accident Investigation 39